F
frwillia
Guest
I had a burr on the crown of my .22-250 which is what got me started tooling up to do barrel work. It looked like this:
I spent the fall and winter getting tooled up, reading, watching videos, and "interacting" here to learn what to do and how to do it.
I cut the crown yesterday after spending some time (like 3 hours of playing around and experimenting) aligning it in the headstock. I used a Grizzly rod and the Gritters method to align the bore near the muzzle. The breech had about .012" of run out on the other end when the bore at the muzzle was aligned. One of the things that took so long was I aligned the chamber end the same way just for fun. With the inch of bore after the throat aligned with the lathe spindle the muzzle was making a 0.056" orbit on the other end.
I cut the crown with a freshly ground and honed HSS-Co bit and pipe threading oil.
It looked like this just before I took it out of the headstock.
With the tooling I made this winter(cat head and spider chuck), this 12x36 Gearhead seems to be a nice lathe for barrel work. As you can see here, the 26" fits nicely and it will work just fine for considerably shorter barrels. The cuts are light for this kind of work so the lathe is plenty rigid, very easy to use, and doesn't take a lot of space.
I bolted my home made barrel vise to the mill table for re-assembling the receiver to the barrel. I only used about 40 ft-lbs of torque on the wrench so this was probably overkill, but the mill didn't move.
Fitch
I spent the fall and winter getting tooled up, reading, watching videos, and "interacting" here to learn what to do and how to do it.
I cut the crown yesterday after spending some time (like 3 hours of playing around and experimenting) aligning it in the headstock. I used a Grizzly rod and the Gritters method to align the bore near the muzzle. The breech had about .012" of run out on the other end when the bore at the muzzle was aligned. One of the things that took so long was I aligned the chamber end the same way just for fun. With the inch of bore after the throat aligned with the lathe spindle the muzzle was making a 0.056" orbit on the other end.
I cut the crown with a freshly ground and honed HSS-Co bit and pipe threading oil.
It looked like this just before I took it out of the headstock.
With the tooling I made this winter(cat head and spider chuck), this 12x36 Gearhead seems to be a nice lathe for barrel work. As you can see here, the 26" fits nicely and it will work just fine for considerably shorter barrels. The cuts are light for this kind of work so the lathe is plenty rigid, very easy to use, and doesn't take a lot of space.
I bolted my home made barrel vise to the mill table for re-assembling the receiver to the barrel. I only used about 40 ft-lbs of torque on the wrench so this was probably overkill, but the mill didn't move.
Fitch